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梅国雄, 宋林辉, 宰金珉. 地下水浮力折减试验研究[J]. 岩土工程学报, 2009, 31(9): 1476-1480.
引用本文: 梅国雄, 宋林辉, 宰金珉. 地下水浮力折减试验研究[J]. 岩土工程学报, 2009, 31(9): 1476-1480.
MEI Guoxiong, SONG Linhui, ZAI Jinmin. Experimental study on reduction of groundwater buoyancy[J]. Chinese Journal of Geotechnical Engineering, 2009, 31(9): 1476-1480.
Citation: MEI Guoxiong, SONG Linhui, ZAI Jinmin. Experimental study on reduction of groundwater buoyancy[J]. Chinese Journal of Geotechnical Engineering, 2009, 31(9): 1476-1480.

地下水浮力折减试验研究

Experimental study on reduction of groundwater buoyancy

  • 摘要: 通过运用模型试验方法,对处于不同环境中深基础上的地下水浮力的力学效应进行分析,主要探讨砂土层和黏土层中的地下水浮力折减情况,并对不同水位下地下水浮力的变化规律和地下水浮力随时间的动态变化过程进行分析。试验结果表明:砂土层中的地下水浮力基本不存在折减,实测值与按阿基米德定律计算的理论值基本相等;而黏土中的地下水浮力实测值始终比理论计算值要小,且水浮力受水位回升的高度和时间的影响,具体的变化规律可用折减系数来表示,低水位下和水位回升初期的折减系数较小,约为0.4左右,随着时间和水位的增长,折减系数逐步增大,最终达到0.70。地下水浮力的可折减性和变化的不确定性表明进一步完善地下水浮力计算理论的必要性。

     

    Abstract: The mechanical effects of the buoyancy acting on deep foundation under different circumstances are studied by model tests.The study subject is the problem of reduction of groundwater buoyancy derived from sand and clay.Moreover,the variation of buoyancy with water level and the dynamic process of buoyancy with time are analyzed.The results indicate that the measured buoyancy of sand is identical with the theoretical buoyancy calculated by Archimedes’s law,while for clay,the measured value,varying with water level and time,is less than the theoretical one.And the difference can be expressed as the reduction coefficient.The reduction coefficient is small,ranging between 0.3 and 0.4,for the lower water level at initial stages.With the increase of time,the value of reduction coefficient gradually becomes large.And it reaches 0.70 ultimately.Therefore,a reasonable design of deep foundation should consider the effect of buoyancy.

     

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