• 全国中文核心期刊
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James Yang, Karin Hellstadius, Malte Cederstrm. 提高大坝安全性能的一种方法——溢洪道维修案例分析(英文)[J]. 岩土工程学报, 2008, 30(11): 1707-1712.
引用本文: James Yang, Karin Hellstadius, Malte Cederstrm. 提高大坝安全性能的一种方法——溢洪道维修案例分析(英文)[J]. 岩土工程学报, 2008, 30(11): 1707-1712.
James Yang, Karin Hellstadius, Malte Cederstr m. Case study of spillway modifications——a means to a higher level of dam safety[J]. Chinese Journal of Geotechnical Engineering, 2008, 30(11): 1707-1712.
Citation: James Yang, Karin Hellstadius, Malte Cederstr m. Case study of spillway modifications——a means to a higher level of dam safety[J]. Chinese Journal of Geotechnical Engineering, 2008, 30(11): 1707-1712.

提高大坝安全性能的一种方法——溢洪道维修案例分析(英文)

Case study of spillway modifications——a means to a higher level of dam safety

  • 摘要: 瑞典新的洪水设计及大坝安全指南对全国水库大坝的安全提出了更高的要求。指南对每一条河流情况进行了复核并找到了较好的解决方案,即储水和提高溢洪道泄洪能力相结合的方案。为了符合指南的要求,瑞典全国上下都在实施一个大坝安全计划,对大量的水库大坝提高其安全性能,以满足更高的洪水设计(及其它方面)的要求。技术方案包括大坝加固、溢洪道泄洪能力提升和临时储水设施。Stenkullafor 水库大坝设有一个 2 闸控制的敞开式溢洪道。该水库修改后的设计洪水将比现有溢洪道泄洪能力提高 40%。根据成本效益分析,提高溢洪道泄流能力的主要措施是降低其中一个闸门顶高程,以适应需要提高的泄洪能力。通过水工模型试验,一方面优化溢洪道顶部轮廓,另一方面降低溢洪道顶部改造和新闸门的成本。溢洪道右侧闸门底高程降低 4.3 m,并新安装一扇更高的闸门。现在,大坝的安全性能已得到提高。对水工模型试验和施工时的洪水风险,施工过程及其遇到的困难进行了介绍,并对坝体加固、上游坡新的侵蚀防护、下游消能及下游行洪渠道等工程措施进行了描述。

     

    Abstract: New Swedish design-flood and dam-safety guidelines require a higher level of structural and hydraulic safety of the existing dams in the country.The guidelines initiated a review of each river to find good solutions-combinations of retention of water and increased spillway capacity.To comply with the guidelines,a dam-safety program undergoes in the country to rebuild a large number of dams to improve their safety-for higher design floods and also in many other respects.Technical solutions include dam reinforcement,spillway capacity increase and temporary storage of water in large reservoirs.Stenkullafors has a spillway with two gated overflow openings.Its revised design flood is 40 % higher than its existing spillway capacity.Based on a cost-benefit analysis,modifying one spillway opening to a lower crest was chosen as the main measure to cope with the flow.Through hydraulic model tests,the spillway crest profile was optimized so as to achieve the required capacity on one hand and to minimize the cost of the spillway crest and the new gate on the other.The sill elevation in the right spillway opening was lowered by 4.3 m and a new higher tainter gate was installed.The dam has now been rebuilt to higher safety level.This paper addresses hydraulic model tests and the risk of flood occurrence during the construction time.Also,the construction process and difficulties that were encountered are described.Other engineering measures are strengthening of the dam body,new erosion protection on upstream slope,energy dissipater and channel downstream.

     

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